Spectre Performance purchased a 74 Maverick, with a 200ci inline six to use as a project car and test bed for their new EMS-Pro fuel injection controller. The motor only had 20K miles since it was rebuilt, but had a severely scored piston in one cylinder. This was causing major blow-by and a loss of compression in that cylinder. Hence the decision was made to pull the six and swap in a V8.
However, before the engine was pulled out and sent off to it's final resting place, Hot Rod...
However, before the engine was pulled out and sent off to it's final resting place, Hot Rod...
You do not have permission to view the full content of this article.
Log in or register now.