A
Anonymous
Guest
Two years after the blunder, it feels SO good -
When I rebuilt my 3.3L/200 CID 2 years ago, I had to put in the Victor head gasket that you get at NAPA. I knew the resulting compression was low, but did not realize just how much these engines rely on their squench bands for higher RPM performance - boys, it's CRITICAL!
When I took out the head gasket, I found it had only compressed about .006" on average, going from .050" when new to .044" afterward. This meant that the compression ratio was only 7.7:1 (original was 8.25:1), but more importantly, the squench height was
(.044"+.025" deck height)=.069", which is to say, no squench at all, since anything over .040" is pretty useless.
Today, I got my engine back together with a .010" head mill, the steel FoMoCo head gasket (thanks, Mustangaroo - ) and a Clifford exhaust port divider. The compression is now 8.6:1 (58cc head chamber) with the .018" thick steel gasket.
My 'test hill' is a very steep 12 degree hill, 1/2 mile long, near my house. Before this modification, I could pull this hill at WOT at a mere 32 MPH (30 MPH before the first rebuild). Today, I bettered that climb by 14 MPH, at 46 MPH and still accelerating when I ran out of hill!
I know from building racing motorcycle engines for years that the squench band is the secret of passing the 9,000 RPM mark, even up to 18,000+ RPM (yes, that's not a typo-), but those are all hemi-head engines. Now I know that the secret of getting better high-RPM efficiency in these 3.3L heads is in the squench, also, despite the bathtub-shaped 'wedge' these heads have.
Oh, one other thing I did - I ported the intakes on just cylinders 1,2,4 and 6 to and matched the new valve seats into the port shape, to balance the flow better. I also unshrouded the valves on all chambers just .030" or less and rounded off the sharp edges that the valve job caused where the new seats were cut into the heads, all with my trusty Dremel tool. I also rounded the boss where the sparkplug protrudes into the chamber, because each chamber's shape was different in this spot. Now they are all similar.
After I start driving it regularly, I'll post the MPG numbers. Before the first rebuild, I was getting 15-16MPG on 85 octane. After the rebuild, it dropped to 14-15 MPG, disappointing at best. Water injection brought it up new 18 MPG on a good day. Now, I'm hoping to reach 18 MPG on 85 octane alone - I'll let you know!
Thanks, too, to Dave - CZLN6 --
- you're the greatest!

When I rebuilt my 3.3L/200 CID 2 years ago, I had to put in the Victor head gasket that you get at NAPA. I knew the resulting compression was low, but did not realize just how much these engines rely on their squench bands for higher RPM performance - boys, it's CRITICAL!
When I took out the head gasket, I found it had only compressed about .006" on average, going from .050" when new to .044" afterward. This meant that the compression ratio was only 7.7:1 (original was 8.25:1), but more importantly, the squench height was
(.044"+.025" deck height)=.069", which is to say, no squench at all, since anything over .040" is pretty useless.
Today, I got my engine back together with a .010" head mill, the steel FoMoCo head gasket (thanks, Mustangaroo - ) and a Clifford exhaust port divider. The compression is now 8.6:1 (58cc head chamber) with the .018" thick steel gasket.
My 'test hill' is a very steep 12 degree hill, 1/2 mile long, near my house. Before this modification, I could pull this hill at WOT at a mere 32 MPH (30 MPH before the first rebuild). Today, I bettered that climb by 14 MPH, at 46 MPH and still accelerating when I ran out of hill!
I know from building racing motorcycle engines for years that the squench band is the secret of passing the 9,000 RPM mark, even up to 18,000+ RPM (yes, that's not a typo-), but those are all hemi-head engines. Now I know that the secret of getting better high-RPM efficiency in these 3.3L heads is in the squench, also, despite the bathtub-shaped 'wedge' these heads have.
Oh, one other thing I did - I ported the intakes on just cylinders 1,2,4 and 6 to and matched the new valve seats into the port shape, to balance the flow better. I also unshrouded the valves on all chambers just .030" or less and rounded off the sharp edges that the valve job caused where the new seats were cut into the heads, all with my trusty Dremel tool. I also rounded the boss where the sparkplug protrudes into the chamber, because each chamber's shape was different in this spot. Now they are all similar.
After I start driving it regularly, I'll post the MPG numbers. Before the first rebuild, I was getting 15-16MPG on 85 octane. After the rebuild, it dropped to 14-15 MPG, disappointing at best. Water injection brought it up new 18 MPG on a good day. Now, I'm hoping to reach 18 MPG on 85 octane alone - I'll let you know!
Thanks, too, to Dave - CZLN6 --
