Today (Sunday) I went back and checked and after removing the exhaust manifold I took a look at the port divider. It was in rock solid. I couldn't budge it. The epoxy was very very hard, much different than yesterday. Idling the engne really cured it.
The headers were hard to get into their position in the engine compartment, but I got it. I put the headers on loose with new bolts and sized where to cut the exhaust pipe by installing it, marking it, and then removing it and cutting it and reinstalling it to check the fit. With the exhaust pipe installed like we wanted it my buddy then tacked on the new exhaust flange. We dropped the exhaust pipe again and he welded it spot by spot to avoid melting through the thin metal. We ground the weld down to look good. We reinstalled the exhaust pipe and it fit really, really well and it much easier to install and remove than it used to be. The pipe was so long before that it bridged over the tie rods straight back to the rear axle and it took some magic to get the pipe off. Now, the pipe doesnt catch over the tie rods any more so it is much easier to remove and install.
My headers were Clifford Headers with a single outlet. I installed the starter from underneath with the headers on and it was very tight to get the starter in. I think it would be impossible from above. I heard some people had issues with clearance of the copper stud that the starter relay attaches to, but I didn't. I then undid the 2 bolts that were holding the headers in and applied some permatex high temp gasket maker to the gasket. I dropped the gasket onto the headers and fastened them to the engine. It was hard, hard to get at the bolts. A racheting box end wrench was invaluable. There were a few bolts that I couldn't get a rachet onto because the header tube was too close and even a u-joint wouldn't make it. It was really tough fighting the bolts in but I won.
After completing this much of the installation I found that the throttle "bar", for lack of a better word, hit one of the header tubes. It kept the engine at part throttle and wouldn't let it idle. This is the little lever that the return spring attaches to and it hit the header tube just below the return spring hole. What I ended up having to do was grind the lever until it was shorter than where the spring hole was and drill a new spring hole. Then the lever worked fine.
Everything sealed up well and it sounds great. I have had an exhaust leak from the old exhaust manifold since before last thanksgiving and it sounds so good now. I think the sounds is a little deeper now that it ever was before. I still have stock exhaust tubing size as far as i know, it is pretty small so I wasn't expecting much change but the car feels good and sounds good so I am happy.
The last thing of note that I can remember now is that I made a tube for the exhaust riser tube. I got a length of 1/4" copper tubing and ran it down to a header tube and rant it along the header tube for a bit like one of the Schjeldahl's recommended to me. I hose clamped the copper tube to the header tube and wrapped the copper tube with some insulating material and hose clamped that on. It looks like a good clean install. I am not sure how well it works now, I have the choke stuck open because I was having trouble with it before. Can't fix everything in one day.
Hope that write up covered all the bases.
-Dan in Atlanta