edgewood bronco
Well-known member
I'm putting this out here so that perhaps other folks can be helped by my experience.
I just got my 66 Bronco with a 170 and an Autolite 1100 carb on the road. I'd had some drivability problems: The truck would stumble when hot around town (25-35 mph), and did not start well when hot. It acted like it was flooded. Lots of cranking with the pedal to the floor would get it going finally.
I've made some changes and this is what seemed to help: I lowered the float about 1/16". I got this idea from my dad who runs old flathead v8s and found that leaning out the float adjustment beyond stock helped.
I also replaced both acclerator pumps. This was necessary because they were leaking so that the bowl would dry out after a couple days, but it also seemed to help the other problems as well.
I had about 200 miles on it since I got it back on the road. The three fillups during that time saw my mileage go from 17 to 16 then 15 mpg. Something was wrong. The plugs were really black and wet and otherwise fouled, and I cleaned them up and got them back to specs as best as I could. I'm driving it as much as possible now, and will re-post when I have an update.
Happy motoring!
I just got my 66 Bronco with a 170 and an Autolite 1100 carb on the road. I'd had some drivability problems: The truck would stumble when hot around town (25-35 mph), and did not start well when hot. It acted like it was flooded. Lots of cranking with the pedal to the floor would get it going finally.
I've made some changes and this is what seemed to help: I lowered the float about 1/16". I got this idea from my dad who runs old flathead v8s and found that leaning out the float adjustment beyond stock helped.
I also replaced both acclerator pumps. This was necessary because they were leaking so that the bowl would dry out after a couple days, but it also seemed to help the other problems as well.
I had about 200 miles on it since I got it back on the road. The three fillups during that time saw my mileage go from 17 to 16 then 15 mpg. Something was wrong. The plugs were really black and wet and otherwise fouled, and I cleaned them up and got them back to specs as best as I could. I'm driving it as much as possible now, and will re-post when I have an update.
Happy motoring!