I have been breaking in and tuning the Clifford built 250 and incrementally making progress. It has been running awesome with a Holley 2bbl and outer carbs blocked while I worked on ignition and other things. I am now re-visiting the Offy 3X1 setup. The engine came with three Holley 1904's rebuilt and clean - somewhat modified linkage, chokes removed and plugged, vac ports plugged. I used my '63 Falcon Wagon's excellent running 170' six for static and road testing the three Holley's after temporarily removing the OEM 1100 carb. The testing included hooking up vac advance and minimal idle A/F tweaking on the 170.
1) The FRONT Holley started, idled and revved well with static test on the 170. Drivability test revealed It stumbled mildly at mid throttle cruise and stumbled continually under load.
[ List 2245S / 11B (1-7/16) Base ]
2) The REAR carb started, idled and revved well static. Ran well on drive test except for leaky needle flooding episode which is minor repair concern.
[ 2?45S 803 / B35 (1-716") base ]
3) The CENTER Holley started but ran rough and only with mix needle all the way out - stalled and revved badly - ran better with finger partially choking venturi. I didn't attempt road test. [2245AS 0143 / E12 (1-9/16") base ]
Although these carbs are never used rebuilds, they had been sitting. I installed "jify" kits in them and got the EXACT same results other than eliminating the leaky float on # 2. I have taken them apart and compared the good running one with the other two for blockage, sealing and operation with no change to the problems with # 1 & #3.
Powerband 8)
1) The FRONT Holley started, idled and revved well with static test on the 170. Drivability test revealed It stumbled mildly at mid throttle cruise and stumbled continually under load.
[ List 2245S / 11B (1-7/16) Base ]
2) The REAR carb started, idled and revved well static. Ran well on drive test except for leaky needle flooding episode which is minor repair concern.
[ 2?45S 803 / B35 (1-716") base ]
3) The CENTER Holley started but ran rough and only with mix needle all the way out - stalled and revved badly - ran better with finger partially choking venturi. I didn't attempt road test. [2245AS 0143 / E12 (1-9/16") base ]
Although these carbs are never used rebuilds, they had been sitting. I installed "jify" kits in them and got the EXACT same results other than eliminating the leaky float on # 2. I have taken them apart and compared the good running one with the other two for blockage, sealing and operation with no change to the problems with # 1 & #3.



Powerband 8)