HELLO 250 COUPE
.....ONE THING ABOUT BEING OLD IS YOU SEEN ALOT OF THINGS. WELL I'VE SEEN THIS DONE BRFORE AND WAS APART OF SOME GUYS WHO MADE ONE THAT WORKED.
.....1956 OR SO....A FRIEND HAD A 1953 FORD. HE WANTED TO TRY AND GET MORE POWER FROM HIS CAR. HE TOOK A KIRBY VACUUN CLEANER AND USED THE IMPELLER AND CASE WITH A STARTER MOTOR
AND PUT ON HIS '53. WE WORKED ON IT FOR OVER TWO WEEK BEFORE WE TRIED IT. DIDN'T SEE MUCH. TOOK IT OFF AND REWORKED IT... 4 TIMES.
.....WHEN IT WORKED YOU COULD TELL THERE WAS SOMETHING HAPPENNING. WE TESTED IT THE WAY EVERYONE DID BACK THEN....WE TOOK IT TO THE ROAD AGAINST OUR OTHER CARS. WE FOUND HIS CAR WAS FASTER THAN OURS. THAT WAS A CHANGE. WE ALL HAD CARS THAT WERE ABOUT THE SAME IN DRAGGING. THE FASTEST WAS A 1952 CHEV. 6 THAT HAD A MILLED HEAD AND BIGGER CARB. AND HOT COIL. THE CHEV WOULD PULL AWAYFROM EVERYONE BY A FULL CAR/LENGTH. THE CHANGE WAS THE 1953 FORD OUT PULLED THE CHEV THE FIRST 60 FT. AND HELD IT.
.....WE ALL FELT IT WAS ONLY GOOD FOR THE FIRST BLOCK OR SO. THE TOP SPEED WAS NOT AS FAST.
..... THE UNIT HAD A HOSE BUILT TO GO TO THE TOP OF THE CARB. THE UNIT SAT ON THE PASS/SIDE. THE CARB SIZE WAS LARGER THAN THE CASE SIZE SO IT WAS NOT A GOOD SETUP. WE ALL THOUGHT IT HELPED AT LOWER RPM'S AND NOT A HELP AT UPPER RPM'S. ALSO WE ONLY RAN IT FOR 12 SECONDS. IT GOT VERY HOT AFTER TWO RUNS. THE LONGEST IT WAS RUN WAS TO 20 SECONDS. THEIR WAS NO HELP AFTER ABOUT 10SECONDS.
.....I RODE IN IT ONCE AND TURNED ON THE SWITCH AFTER IT WAS GOING IN SECOND GEAR AT 15 MPH AND THEIR WAS A CHANGE.
.....I WOULD GUESS IT HAD 8-10 MORE HP. THATS ABOUT 6%. NOT MUCH FOR ALL THE WORK. BUT IT WAS FUN TO TRY SOMETHING LIKE THAT.
.....MY BLAST FROM THE PASSSSSST.
LIVE IN GRACE
LEROY POLL