Ok, so I tried a 55 idle jet and taping up the hole. I was able to readjust my idle mix and speed screws down but it was running like.... well you know. I only did a mile or so at 30 mph, but it was bogging while shifting and the AFR was jumping around. Not sure if the tape was leaking or what. I put the 70 back in, removed the tape and readjusted the screws, runs good again.
I might order a 75 & 80 idle jet and try later this week. It was 95 -100* in LA today, not your ideal under-the-hood weather.